I purchased a atom v3 kit and assembled. I flew it for thirty seconds indoors with the receiver taped to the bottom for testing and it flew great. I then put the receiver under the canopy and bolted it down which crushed the flight controller. This was a colibri race 2.0 flight controller.
I ordered a new corlibri race 2.0 flight controller and installed. I calibrated the esc board. Calibrated the accelerometer. When arming the motors rattle while spinning and get very hot immediately. However when using the motor spin feature in betaflight they don't rattle and do not heat up. The motors individually randomly go full throttle when armed verified by viewing the motor live data section in beta flight. Also the accelerometer shows the craft is randomly pitching and rolling however it is not. The accelerometer does not show random pitching and rolling when using the motor control in betaflight.
I installed the original receiver and installed a second to rule out a receiver issue. I have also installed the latest firmware available.
I am unable to recover the dump from the original flight controller therefore cannot transfer it to the new one.
Does anyone have any ideas where to go from here?